Traffic flowing again after a dispatcher's nightmare

Looking at this photograph of hot intermodal CSX Q026 passing a tied down CSX W017 rail train just north of the yard at Guthrie, Kentucky on the Henderson Subdivision, you wouldn’t know what transpired over 7 hours before their arrivals here! Well, here’s what happened!

On March 20th, 2021 at approximately 9am CSX Q513 (12,000+ feet long) was about halfway through Adams, Tennessee when their train ripped a coupler completely out of a refrigerated car about 2/3 through their train and went into full emergency, which ended up causing a major problem on the Henderson Subdivision!

Since the train separated on the main, nothing could get around it and before it was over all four hot intermodals on the Henderson Subdivision, Q029, Q025, Q026 and Q028, were now delayed, as were many other trains, including this rail train as a result!

They finally figured out a plan that worked where the power from Q029 was brought up from Guthrie, Ky and hooked onto the rear of Q513 to hold the last 1/3 of Q513 in place. 

Q513 then pulled the front 2/3 of their train south into the siding at Cedar Hill, Tennessee where a bracket was welded onto the reefer car, to hold the EOT device, as a new coupler couldn’t be installed due to the damage.

The power on Q513 then pulled away from its train at Cedar Hill, where it went out the south end of the siding and back north on the main to pickup the rest of its train. 

They then brought the rest of Q513 back to Cedar Hill where they backed into the siding and hooked onto the rest of their train. By this time the crew was now out of time and they the train down, till a fresh crew showed up later to take it on south.

Finally, Q029, Q025 and loaded a loaded coal train went on south where Q026 and Q028 were waiting to come north, and the railroad got to moving again!

As a result of all this, the rail train, which sat at the south end of Trenton, Ky for all this time, ended up being brought on up to Guthrie where their train was also tied down just short of the crossing at Park Street. 

The crew was sent to a hotel and I’m not sure if it’s because they ran out of time or if the dispatcher didn’t want a slow speed train (30mp train and 10mph through turnouts and sidings) on the line as everything had been backing up for six hours! 

Just another day on the railroad!!

Tech Info: DJI Mavic Air 2 Drone, RAW, 4.5mm (24mm equivalent lens) f/2.8, 1/500, ISO 100.

Traffic flowing again after a dispatcher’s nightmare

Looking at this photograph of hot intermodal CSX Q026 passing a tied down CSX W017 rail train just north of the yard at Guthrie, Kentucky on the Henderson Subdivision, you wouldn’t know what transpired over 7 hours before their arrivals here! Well, here’s what happened!

On March 20th, 2021 at approximately 9am CSX Q513 (12,000+ feet long) was about halfway through Adams, Tennessee when their train ripped a coupler completely out of a refrigerated car about 2/3 through their train and went into full emergency, which ended up causing a major problem on the Henderson Subdivision!

Since the train separated on the main, nothing could get around it and before it was over all four hot intermodals on the Henderson Subdivision, Q029, Q025, Q026 and Q028, were now delayed, as were many other trains, including this rail train as a result!

They finally figured out a plan that worked where the power from Q029 was brought up from Guthrie, Ky and hooked onto the rear of Q513 to hold the last 1/3 of Q513 in place.

Q513 then pulled the front 2/3 of their train south into the siding at Cedar Hill, Tennessee where a bracket was welded onto the reefer car, to hold the EOT device, as a new coupler couldn’t be installed due to the damage.

The power on Q513 then pulled away from its train at Cedar Hill, where it went out the south end of the siding and back north on the main to pickup the rest of its train.

They then brought the rest of Q513 back to Cedar Hill where they backed into the siding and hooked onto the rest of their train. By this time the crew was now out of time and they the train down, till a fresh crew showed up later to take it on south.

Finally, Q029, Q025 and loaded a loaded coal train went on south where Q026 and Q028 were waiting to come north, and the railroad got to moving again!

As a result of all this, the rail train, which sat at the south end of Trenton, Ky for all this time, ended up being brought on up to Guthrie where their train was also tied down just short of the crossing at Park Street.

The crew was sent to a hotel and I’m not sure if it’s because they ran out of time or if the dispatcher didn’t want a slow speed train (30mp train and 10mph through turnouts and sidings) on the line as everything had been backing up for six hours!

Just another day on the railroad!!

Tech Info: DJI Mavic Air 2 Drone, RAW, 4.5mm (24mm equivalent lens) f/2.8, 1/500, ISO 100.